January 2005 |
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01/01/05
- Where did the year go? Today Royal, Roxane and Dan took down
the Christmas lights. Roxane continued removing the linoleum on
the pilot house deck.
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Dan got the screws
out of the AC panel that were being a bear to remove. Two light
fixtures were removed for later repair. More sorting of the
cabinets and hardware for the crew areas was done |
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5 - Puget Sound Maritime
Heritage Society - As guest speaker I presented a PowerPoint
presentation of the history and the trip up the coast of the
83527. |
Winter Scenes |
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Harbor Guardian |
Olympic Mountains |
Tied at "a" dock |
Coast Guard working on light at harbor entrance |
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8-9
Scraped more linoleum.
Dean Lachaw, a retired 6-71 engine volunteer visited to see what
was going on with the smoking engine. After a valve adjustment
we were still smokey. Closer analysis showed that the oil was
completely contaminated with water. We started draining the pan. |
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15-16 - Pacific NW
Maritime Heritage Council Meeting - Presented the status of the
project. |
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22-23 - We got to
the boat about 8:45 and the wind was really howling. We had
to re-tie the boat because it was pushed about 4' from the dock.
One cleat was almost ripped out on the aft quarter. It took 4 of
us about 1.5 hours to get the lines changed and re-secured.
Roxane and Carol Craig spent most of the day scraping linoleum
glue in the crew quarters. Slowly we are winning that battle.
Ed Young, former 83527 sailor
stopped by with a great photo
from his days aboard.
Dean Robins 6-71 buddy and his friend from Hadlock, WA arrived
about noon. He adjusted all of the valves with the engine cold
per the spec. After starting it still blew white smoke. Oh, no
look at the silver brown oil streaming out of the valve cover.
Water in the oil! Yes, there is a fresh water leak somewhere. It
could be the oil cooler, heat exchanger or engine head. So that
creates another project. Tike is going to talk to a Manson 6-71
engine guy and see what usually goes wrong. Dick is going to
contact an engine guy he knows and get some more opinions and we
will invent a game plan with more info.
Aaron (ham radio friend and AVR fan) came to work on the
generator voltage regulator circuit and discovered that there
were 2 more bad resistors. It appears that corrosion is killing
them. I don’t know if it was a problem from when the saltwater
spray was everywhere when the waterpump was bad, before we got
the boat. Anyway, Aaron will continue attempt to resolve that.
He at least had time to draw up a schematic of the circuit.
We adjourned about 4pm and had a great dinner with Tike and
Margaret, Dick and Carol, Royal and Sue and Rox and I. We had
never been with Margaret, and she was fun and interested in
helping out in the future. Carol and Sue had grown up in a
nearby neighbor hood and gone to the same school at the same
time. I'm not sure if they remembered each other from then
though. They had fun |
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27 - Pulled an oil sample
to take to Caterpillar for analysis. We learned that there was
no salt water in the oil. |
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28 - I received the follow
letter and photo story today
from Joseph A Wright, Jr.
CDR, USCGR (Ret) |
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29 - Scanned
Sea
Classic Magazine Article on 83 Footers
article |
3-1 Earlier in
the month I noticed an ad in
Western Maritime newspaper selling two Detroit Diesel
engine hulks with "crashbox" transmissions
as spares. The deal included two 200 gallon water tanks and two 400
gallon fuel tanks that were pulled out of a 63 foot crashboat
owned by Scott Bennedict in Bethel Island, CA. |
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On Tuesday I scouted out the location of the
equipment. Wednesday met my buddy, George Burton in Vallejo, CA
with his Chevrolet Duramax Diesel pickup and a borrowed trailer.
Thursday we finalized the loading
and in the late afternoon we headed for out for Seattle. At a
"snack" stop in Red Bluff we noticed a stream of diesel
underneath the pickup and trailer hitch. The exhaust pipe was
dripping with diesel. When he pulled the dipstick we saw
that the pan was also full of diesel. George found a yellow
pages in the payphone book and we saw that a Chevrolet/GMC
dealership was 20 miles back south in Orland, CA. So back we
went, but by then the dealership was closed. We then took refuge
in the "Amber Light" motel on the Westside of town waiting for
morning.
At 8 am we were on their doorstep
hoping for a "GM warranty" miracle. Apparently this was a common
problem for the early Duramax engines. There was plenty of
"factory warranty" remaining, so there was little worry about
getting the work done, but the concern was "when" would it be
done. If we had to scrub the journey George would just
take me to the Sacramento airport in a rental car and I would
return home. The dealership really went to bat for us and
by 11am we were on the road with a rental Duramax pickup. Plus,
GM was picking up the rental charge. Although it was not a 4wd
we were not expecting any weather that would require the extra
traction.
George and I had
a great time gabbing and telling sea stories and just drove
straight through to Seattle, actually Port Ludlow and my home at
1:30am.
Two or Three days
later we started offloading the engines from the trailer.
Unfortunately the John Deere tractor with loader that I had
arranged for could not pick up the engine/transmission
combination. So, we had to drag them off of the trailer onto 4X4
boards to then skid them into place where I was storing them.
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Off loading engines at Port Ludlow |
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6-11
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During this week George volunteered his time to assist with the
identification and modification to the AC electrical circuits.
We got some circuits marked for removal and some split or
relocated and documented. Although there is a long way to go it
was a HUGE start to get the elementary drawings completed. |
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12 - This work party was low key. It was mostly
electrical system wrapup and lower deck linoleum cleanup. Tike
Hillman and Mike Mallet put some time into defining the extent
of damage to the bottom of the spray shield. The major goal is
to reduce or eliminate water from seeping down from the overhead
into the crew compartments. George got the bilge/fire pump
rewired and tested. |
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Tike and Mike inspecting the base of the spray
shield. |
Testing the replaced and rewired bilge/fire pump.
Here we are pumping raw water from the thru-hull at the keel
over the side. |
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13 - George left for
home on Sunday. |
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17 - I received this email from David
Bouker today:
Dear Sir:
Larry Eastman (ENC, ret.) a former shipmate on the USCGC
Bittersweet (WAGL 389)
sent me a copy of the July 2004 Retiree Newsletter in
which I was pleasantly surpris-
ed to see an article about the 83 footer that I served on
for a short time in Tacoma,
Washington in 1951. At that time, it was tied up at a dock
just north of the 11th St.
bridge and only a short distance from downtown.
Members of the crew included the following incomplete
list:
Barton BMC
Kroll ENC |
Laqua, Jewel EN2
Davenport SN |
Reichart, Pete SN
Bouker, David SN |
There was a cook and another engineman
whose names I do not recall on board her. I do recall that
it had two 700HP Sterling Viking gas engines. It was
absolutely necessary for the engineman on watch to run the
blowers first for a specified length of time before
starting the main engines.
My time aboard was from January, 1951 to approximately
June of 1951. I took the month of March off to attend a
couple of service schools and was subsequently transferred
to COTP, Portland, Oregon. I was discharged as BM3 in July
of 1952.
Hope this all helps. - David
David Bouker [d-j-bouker@nushtel.net] |
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19-20
- Started the engine oil change, adding kerosene to flush.
Changed the drain plug to a ball valve for ease of draining.
Thompson fixed aft vents to spin open easily and added fans for
air circulation. We had a walkup guest, Franz Gruber, from Port
Ludlow. He served on the 83527 in the early 60's. |
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22 - Craig and
Withers decided the starboard starter was not up to the task and
took it to Townsend Electric for a rebuild. visited BM2 Whitney
Crookham at
Coast Guard Station Port Townsend and got the real color info on
the CG Buff paint color. It is officially "Jarvie Spar Buff"
24635, Color Code 10371. (Sample below) |
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24 -
finished scanning the Twin Disc Installation and
Maintenance Manual and Detroit Diesel Manuals placed online here. |
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26-27 - We
removed deck plates in the Chiefs, galley and
crew berthing compartment and took them home to strip off the
hardware and linoleum. See the photos here. |
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Brass edges need stripped of 50 years of crap and
polished. Most of the screws broke off and were "punched"
through the backside. |
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28 - Chuck
Fowler on behalf of the Tacoma Working Waterfront Museum (WWFM)
discovered that the USS Wabash, AOG-5, a WWII Gasoline Tanker
was due to be scrapped out. It has been tied up at the
Suisun Bay Reserve Fleet (SBRF)
in Benecia, CA for 50 years. SBRF is the west coast storage
location for
MARAD the US-DOT
group that manages the
reserve fleet. The
actual facility can be seen from this
GoogleMaps view. The actual boat is no
longer here. It has been demolished in Texas.
The Wabash was built in
Tacoma in 1942 at the Todd Seatac facility and several
volunteers and friends of the WWFM actually worked at the
shipyard on the ship.
Our mission was to visit
with Earl Johnson, the Fleet Operations & Maintenance Officer to
gain access to the boat and find some artifacts for the WWFM to
commemorate that boatbuilding effort. We arrived at the office
about 13:00 for the initial briefing about how the process works
to go aboard one of the boats.
This letter from
Luke Curtis, the 3rd amigo, will sum up the adventure.
This
slideshow
of the trip is composed from many
photos taken by Dan and Luke.
Part of the afternoon of the first day was
spent at Mare Island visiting Mike
Stone and the USCGC Alert. Mike is part of a group that
is planning to restore the Alert and bring her up the coast to
an Oregon or Washington shipyard for some work.
Luke and Dan were leaving on Tuesday
afternoon. On the way to the Oakland Airport we
swang through the Berkeley Marina
to find an 85' Crash Rescue boat moored there.
The advantage for the 83527 was that a pair of
12" signaling search lights were located and a request for
additional items was made to MARAD. A second road trip is being
organized to get the items for the WWFM and CCOA/83527.
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March 2 - Port
Ludlow Chamber of Commerce PowerPoint presentation held at the
Harbormaster Restaurant. A short tour of the boat followed after
the presentation. |
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5 - Workparty -
Dick Craig rebuilt the stbd 12vdc box to get the missing 1vdc
lost in the connections. Roxane and Carole were preparing
the spray shield for
painting. Dwayne Thompson continued to rewire the aft lighting
circuit. Later the electrical panels were sandblasted at Vern
Perryman's garage. We added a temporary plywood aft hatch that
would be waterproof to keep the lazarette dry since the white
canvas was removed. |
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7 - I attended the
Tall Ships "Maritime Traffic" planning meeting at the Foss
Waterway Office, Tacoma with Dick Craig. The
agenda is here. |
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5-9 - We have been
working off and
on repairing the scuppers under the spray shield. For years the
rainwater has been running through the scupper holes and leaking
down into the compartments. This was repaired by digging out all
of t he soft rotten wood possible, then allowing the areas to
dry out and apply a heavy mixture of fiberglass resin sold by
the
Rot Doctor. Their
documentation is very complete and helpful for just our kind of
project. After 3-4 applications of resin to the troubled areas a
short PVC pipe was cut to length to route the future water
through, instead of a wooden path. |
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We then foamed in the voids with spray can closed
cell foam. The excess was cut away with a knife and "sculptured"
with a Dremel grinder. The outer foam surfaces were fiberglass resined several times. finally the entire lower two inches was
waterproofed with liberally applied black pickup "bedliner." |
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All hangers and hardware removed and the rusty
areas were sanded and a coat of NAPA rust converter was applied.
The seam where the angle iron plate that attaches to the pilot
house and the spray shield was chipped and sanded and all
caulking, bad wood and general crap was removed. The rusty edges
of both sides were painted with the rust converter. More work is required to finish
this part. The final fix will be completed another day. |
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Pilot house seam |
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Aft end of sprayshield |
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Ventilator sheet metal awaiting replacement. |
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9 - Bill Eldridge
from Port Ludlow and former CG EN2, came by and helped tear down
the engine to remove the head for inspection.
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Tearing her down |
Bill removing the head "nuts". |
Early observations |
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15 - I went to the
dock to figure out a way to get the head out of the boat with
limited help. Across the dock from the 83527 was the
USCGC Orcas
from Coos Bay, OR, in for a little R & R on the Port Ludlow golf
course. |
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Orcas across the dock. |
Thanks to Greg Edney, MK2 and Jeff Siron, MKC for
the assistance. |
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16 - Took the engine head to Courtwright
Diesel Machine, [Bill, service manager, 253-383-4888] in Tacoma for inspection.
Chuck and I presented the 20mm
cannon mockup build idea to Andy Barr at WWFM for study and possible
construction from wood. |
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18 - Dick Craig
picked up the head from Courtwright Diesel for the Saturday work
party. |
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19 - At this workparty we got the engine
head into the engine room, discuss moving with PL Marina. sanding
done on the sprayshield. The most fun was getting to paint the stern numbers. |
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Layout and painting the stern numbers |
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Lowering the engine head. |
The ammo lockers before paint chipping and
scraping. |
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26-27
- The weather was raining all weekend. Nothing significant
happened on board. |
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29 -
Dick Craig and Dan started re-assembly of the engine. We got the
head "yarded" over the engine with a chain hoist and a big
c-clamp attached to an overhead beam. It is now torqued down to
spec ready for the injectors to be installed. |
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30 -
Hurray, the Port Ludlow Marina has cut us a break and we can
stay one more month, but at a different slip. That move will
probably take place tomorrow with the help of Mike Mallet and
the Vessel Assist boat. |
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